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									DIY High Flow 8V Head 
									
									
									I certainly am not an authority but I have 
									spent a lot of time researching and testing 
									8V 951 heads in a quest to develop a low 
									cost solution for larger motors. 
									 
									Obviously the 16V is the best solution but 
									the cost is significant and in many cases 
									not practical. I wanted to do a head that 
									would perform well and keep in  
									line with the spirit of low cost Hybrid 
									Stroker motors. Outlined in this thread is 
									my current progress. Much thanks to all who 
									have helped me along the way, especially Sid 
									and MM.  
									 
									The results and the total cost of the effort 
									are also outlined below: 
									 
									951 
									Head.........................................$0 
									(head from my 2.5L) 
									47mm +2 
									Valves..............................$108 
									(set of 4,
									
									see here) 
									Valve 
									Guides....................................$34 
									Valve 
									Seals......................................$36 
									Valve 
									Springs...................................$84 
									(set of 8,
									
									see here) 
									Install 
									Guides...................................$160 
									Remove Valve 
									Seats.........................$48 
									Install New 
									Seats.............................$100 
									Surface 
									Cut......................................$60 
									Competition Valve 
									Job......................$265 
									Total Cost................$895 
									 
									 
									I started with the 8V 951 head from my 2.5L. 
									I disassembled the head, cleaned it, and 
									carefully inspected it. I inspected the 
									ceramic exhaust ports, inspected the deck 
									for pitting in the seal ring areas, 
									inspected how much the head had previously 
									been decked. Some may laugh but below is a 
									picture of my valve spring compressor. It 
									consists of an 8" C clamp from Harbour 
									Freight and a modified socket (total cost $9 
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									The next step was to do the initial porting. 
									I did much of the porting before the new 
									guides or intake seats were installed. In 
									this way I did not have to worry about 
									damaging the guides or the seats while 
									removing much of the port material. The 
									approach I took to porting was two fold. 
									One, to clean things up especially in the 
									throat area. I found on the flow bench that 
									cleaning up the bowl area right above the 
									throat resulted in improved flow. Secondly, 
									to increase the size of the intake port to 
									accommodate the bigger intake valve. My 
									approach was to maintain the port shape 
									while making it bigger. The intake valves I 
									used were 47mm which are 2mm bigger than the 
									stock intake valves. Therefore my approach 
									was to remove 1mm from all the walls of the 
									intake port as shown below.   | 
								
								
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									Below is a picture of all the tools I used 
									for doing the porting. All of the tools were 
									purchased at Harbour Freight with the 
									exception of the inside calipers and the 
									carbide bur (McMaster 4324A32). My porting 
									technique was slow and careful. I took A LOT 
									of initial measurements using the inside 
									calipers. I also used a technique in which I 
									used a drill bit to make several 1mm deep 
									holes as guides for how much material to 
									remove. I removed quite a bit of material 
									from around the guides. Be careful not to 
									remove too much material in the lead up to 
									the guide (see yellow circle above). I 
									probably spent over 20 hours porting the 
									intake ports. It is very important to make 
									the ports as similar as possible in order to 
									promote equal flow. My ports flowed within a 
									few cfm of each other on the flow bench.  | 
								
								
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									Once the initial porting was complete, the 
									head was taken to the machine shop to have 
									new guides and intake seats installed. I had 
									the machine shop bore out the seat throat to 
									within 0.005" of the final throat dimension. 
									I had them bore down into the bowl as shown 
									below as a guide for porting the bowl. At 
									this stage I completed the porting of the 
									intake ports.  | 
								
								
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									I also cleaned up the exhaust ports both 
									around the seats and at the header interface 
									using sanding rolls as shown below. The 
									ceramic often does not line up with the 
									casting and this can be smoothed out to a 
									large extent.  | 
								
								
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									I also did some work to the chamber to 
									de-shroud the intake valves. My bore size is 
									102.3 mm and therefore I could remove some 
									chamber material. I used the head gasket to 
									determine how much material could safely be 
									removed. I marked the deck with a Sharpie as 
									a guide then used sanding rolls to remove 
									material as shown below. I was very careful 
									not to damage the seats.  | 
								
								
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									Once this work was completed, the head was 
									send back to the machine shop to have the 
									valve job done and to be assembled. The 
									valve job is SUPER important. Choose a shop 
									wisely. The intake dimensions I used were 
									developed by blown 944 (Sid) and I used them 
									with great results.  | 
								
								
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									The intake valves are one piece valves and 
									were purchased from SI Valves for $27/each. 
									SI has stock intake valves (45mm) and +1 
									(46mm), +2 (47mm), and +3 (47mm). I used 
									47mm valves due to my bore size (102.2mm). 
									On my flow bench I found very little 
									improvement in flow was obtained above 47mm 
									for my bore size. The exhaust valves are the 
									stock sodium filled valves.  | 
								
								
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									Shown below are some basics with respect to 
									valve springs. The first head I built, I was 
									pretty ignorant to these details. Do your 
									self a favor and get familiar with this 
									diagram. Do not assume the shop you use will 
									get the details right. Verify EVERYTHING.  | 
								
								
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									I was intending to run a high lift cam 
									(0.525" intake lift) and using the formula 
									above it became clear that the stock springs 
									were going to bind. In an effort to find a 
									low cost solution I was able to find some 
									springs for a Datsun 280Z that fit perfectly 
									in the stock retainer and spring cup and 
									provided a bit more seat pressure (138 lbs 
									vs 130 lbs) while having 0.065" more spring 
									travel. The springs are made by Isky Cams 
									(ISK7005-8). As an added bonus, the springs 
									are half the price of the stock springs.  | 
								
								
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									I was able to measure combined coil bind 
									length using a vise and calipers as shown 
									below. Coil bind clearance would be defined 
									as the amount of spring travel remaining 
									before coil bind at the minimum spring 
									height. A safe minimum coil bind clearance 
									would be 0.060". Some have run as low as 
									0.030" coil bind clearance in race 
									environments. Running these low of 
									clearances requires real precision in 
									determining the physical dimensions of each 
									valve. Also, keep in mind that as clearance 
									is reduced, spring life is also impacted.  | 
								
								
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									I had the head decked a few thousands just 
									to clean things up for the Cometic MLS 
									gasket.   | 
								
								
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									The completed head was flowed on a Superflow 
									flow bench at 28 inwc and the results are 
									shown below. The results show that cleaning 
									up the exhaust port and having a proper 
									competition valve job makes a huge 
									difference in an already outstanding exhaust 
									port. Also, the larger valve size in 
									conjunction with proper seat and throat 
									dimensions resulted in significant 
									improvement in intake flow.  | 
								
								
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